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You might consider plugging that back in and using a battery tender. Almost seems like the car was struck by lightning. The wiring and grounds are good but the modules/computers are all going bad it seems.I was having trouble with bad batteries every 6 to 12 months. Once I disconnected the whole monitor on the negative battery cable that problem on the way and has been fine for years.
I did that last week. I have an analyzer at home and also took it to advance auto. no issues found.Why not pull the battery and take it to have tested as @swathdiver suggested?
I’m out for a drive now. Drove it long enough to get it out of closed loop. Stopped for lunch and we’ll seewith that many codes I would have to guess there is a short in the lan buss or a module is bad or going bad works until it gets warmed up then shorts out.
it's probably going to take a deeper diagnostic to figure out. meaning like testing on the lan buss with a scope and that takes a certain skill set.
just my .02
Did that this morning. Everything looks good.Maybe check the fuse box, pull it off and see if there is any corroded pins.
Is your battery an AGM? I just went through a whole series of electrical gremlins on my Infiniti G35X, which had a 10 month old AGM battery from Advanced Auto. Took it to them for testing and it all tested fine on their 1990s tech battery/charging system tester so they wouldn't replace the battery. Just the same, I went down the street to Autozone and bought a new conventional lead-acid battery and put it in. All problems magically fixed themselves.Well, the saga continues.
I replaced the terminal ends of the negative ground cable from the battery to the block/front bumper and discovered the inside of the cable was black and had a green dusty substance as well.
Installed the new battery to block/frame ground today. Frame grounding points are clean. The secondary ground at this same location looked good, but i went ahead and put a new terminal end on it as well.
I also re-did the ground wire under the driver side door; removed the end and spliced in a new loop terminal.
Everything was good, let it run and all the codes were gone with the exception of the transfer case.
After a hot -soak and restart, “engine power is reduced” message is back again.
FML.
Removed the top cover of the dash and verified the ground wires were clean and secure.
So the following has been performed:
Throttle Body (new OEM)
Negative Battery cable (OEM)
Battery is good
Every ground checked, cleaned and reassembled.
No evidence of wire damage
Fuses / relays all pulled and verified there is no corrosion
WHAT am I missing?
I’m half temped to either take it to the dealer or just sell the damn thing.
We have had some cooler weather, it is not doing it nearly as frequently. Specifically when it’s cold – cold for Florida under 60° – it will do it every few days.What happens if you do the heat soak repro with the hood open?
Might be a way to start blaming the ecm since it's under the hood.