Traction control/stabilitrak off issue

Disclaimer: Links on this page pointing to Amazon, eBay and other sites may include affiliate code. If you click them and make a purchase, we may earn a small commission.

Marioski

Full Access Member
Joined
Aug 31, 2012
Posts
101
Reaction score
3
Location
IL
Nice job! Hopefully that cures the problem and the electrical gremlin goes away. All I know is that on these trucks if there is any voltage drops they start doing all sorts of weird things

As far as the Airaid tube popping off, I wonder if it's weather related and attributed to the colder temps. I'm going to have to do a google search on that.


Sent from racephone
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
Me too! The CEL and traction control lights going away is typical after you pull the battery cable though...for a day or so. At least that's how long they've taken to reappear in my case. The P0172 and P0175 codes (banks 1 and 2 too rich) take a while to register because the computer tries to compensate. When it can't compensate any longer, it throws the code. If I get through the next couple of days without any issues, then I'll break out the champagne. :D

Thanks for the tips on the cables, I really hope that did it.
 

Marioski

Full Access Member
Joined
Aug 31, 2012
Posts
101
Reaction score
3
Location
IL
Hell mine came back almost immediately. Plus when my stabilitrack/service 4wd would flicker on / off, everytime it was on the trans would have a very hard shift from 1st to 2nd. It was def an electrical gremlin and I figured it's either a bad ground, bad positive connection or a bad connection somewhere by the body control module.

I've been going good since Saturday morning and have put about 300 miles since then.

It'll be interesting to hear your update.


Sent from racephone

---------- Post added at 11:12 PM ---------- Previous post was at 11:07 PM ----------

Huh. Interesting. Quick google search yielded these results for the MIT tube popping off. Seems it's common. Interesting

http://www.silveradosierra.com/vortec-5-3l-v8/airaid-mit-is-popping-off-t79538.html

And this one.

http://www.silveradosierra.com/vortec-5-3l-v8/airaid-mit-t72410.html




Sent from racephone
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
That's why I thought it was an intake problem or an intake leak - the hard shifting is part of a "safe mode" that the computer goes into when the MAF is disconnected or there is a vacuum leak. My '00 Yukon did the exact same thing when I installed an AEM Brute Force on it but forgot to plug the MAF sensor harness back in. If there is un-metered air getting into the motor, the computer flips out and maxes out the line pressure resulting in crazy shifts (I didn't have the stablitrak off/traction control issues on that truck because the 2000's didn't have either system...but I'm sure that it's all part of a cascading system shutdown to prevent engine/trans damage when something isn't working correctly).

So, based on that experience, naturally I thought that the whole thing was caused by the intake tube popping off and causing a massive vacuum problem. When the issues came back even with the intake put back on correctly, it threw me for a loop. If polishing up the battery/fuse connections really does do the trick, I haven't a clue as to why. The whole thing starts with the airaid tube popping loose, and is fixed by messing with the battery cables? It's a strange problem, to say the least. Great to hear you've gone so long without having an issue though, that is really good news.

Gotta love computer controlled trucks. ;)

ETA: Might be selling my Airaid and shelling out the dough for a Volant. Sheesh.
 
Last edited:

Marioski

Full Access Member
Joined
Aug 31, 2012
Posts
101
Reaction score
3
Location
IL
Ah... I figured it was some sort of safe mode that the truck was going into but glad it's confirmed now.

You're right, any rich or lean code is always a vacuum leak. Could be something minor like a loose line down a to a cracked plastic manifold. It's just interesting that I have ran the MIT tube for several months now with no issues and all of a sudden it popped off.

Sent from my iPad using Tapatalk HD
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
Well, back to the vacuum leak theory. Codes/warning lights came back immediately on my way to work this morning. I'll be chasing it down this weekend if I have time.
 

felixgun

Full Access Member
Joined
Oct 7, 2010
Posts
9,746
Reaction score
136
Location
Lafayette, LA
Shit... I'm having the CEL/Tracking Control/Stabilitrak issue, along with the hard shifting... hopefully it's just the loose intake tube that's creating a vacuum leak.
 

SmallXL

Full Access Member
Joined
May 20, 2010
Posts
104
Reaction score
1
Yup, my airaid popped off as well... grrr.

Threw the lean condition code. Makes sense as it's getting too much air to compensate for fuel at the MAF?

Re-connected and everything was okay after reset.

Could be reading rich until it relearns the actual condition with it connected? Did you re-connect the re-circ/vacuum line?
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
If you're referring to the line that runs from the center of the tube to the passenger side of the engine, it never came loose...just the tube itself popped off at the throttle body.
 

zunman

TYF Newbie
Joined
Feb 2, 2013
Posts
8
Reaction score
0
After hard down shifting issues in tow haul mode when the truck is cold, and also the same traction control and stablitrac service alarm on the display, I ended up finding my 3/8 tube from the tube to the intake manifold on my cheap ebay aluminum intake was dry rotted and disconnected (after it was at the dealer for trouble shooting the tranny issue) They said the truck shifted fine too…. I replaced the line and it has not had the alarm again in 20 miles, I have not driven it in the cold to see if it is down shifting hard yet tho. Hopefully the tube was it, it was also throwing the 2 lean codes like you all are speaking of! Check for a vacuum leak!!!!!
 

zunman

TYF Newbie
Joined
Feb 2, 2013
Posts
8
Reaction score
0
After hard down shifting issues in tow haul mode when the truck is cold, and also the same traction control and stablitrac service alarm on the display, I ended up finding my 3/8 tube from the tube to the intake manifold on my cheap ebay aluminum intake was dry rotted and disconnected (after it was at the dealer for trouble shooting the tranny issue) They said the truck shifted fine too…. I replaced the line and it has not had the alarm again in 20 miles, I have not driven it in the cold to see if it is down shifting hard yet tho. Hopefully the tube was it, it was also throwing the 2 lean codes like you all are speaking of! Check for a vacuum leak!!!!!

never mind my truck still seems like the throttle is out of calibration, spoke too soon. Im starting to not like this truck…ugh I give it a bit of throttle and it feels it wants to launch on its own some times. Back to the tuner I guess. Maybe its the tune or my throttle position sensor is going.
 

Factory909

TYF Newbie
Joined
May 16, 2013
Posts
10
Reaction score
0
I had the same issues as you guys did with my '08. CEL lights, 4x4, etc lights going crazy, running rough. Jiggle the battery cable and all was fine, until the next time. Question, are you guys still running the stock battery terminals? I found another post on here, and was my reason for joining, that a guy was dealing with sort of the same thing. I replaced both the neg and pos terminals with aftermarket ones. What I found when I cut them open was scary. There was ALOT of arcing going on in the neg terminal, where it has the main neg cable along with the little cable. I diced it open and there was alot of blue in there where you could cleary tell it was arcing out. Once I replaced them with some good audio system connectors (I think $20-$30 from Autozone) I haven't had a problem since.
 

Bogart

Member
Joined
Mar 31, 2013
Posts
57
Reaction score
0
Had my airaid a few months and the check engine came on last week. When driving home from work the truck sounded horrible. Popped the hood and noticed the tube hade come off. Hope this is not a recurring problem.
 

strokinpower

Full Access Member
Joined
Apr 23, 2013
Posts
195
Reaction score
1
Well you can clean the boot up really well and the throttle body and squirt a little hair spray on it and it wont budge. Works on intercooler boots on diesel trucks so I would think it would work here.
 

felixgun

Full Access Member
Joined
Oct 7, 2010
Posts
9,746
Reaction score
136
Location
Lafayette, LA
Had my airaid a few months and the check engine came on last week. When driving home from work the truck sounded horrible. Popped the hood and noticed the tube hade come off. Hope this is not a recurring problem.

Just wanted to note on this thread that the same exact thing happened to me. CEL is still on but stabilitrak and traction control issues went away. This MIT sucks apparantly.
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
Well you can clean the boot up really well and the throttle body and squirt a little hair spray on it and it wont budge. Works on intercooler boots on diesel trucks so I would think it would work here.

Good tip. Finally...a use for my wife's smelly hairspray that I can actually enjoy, lol. How hard is it to pull the tube off for maintenance when the time comes?

To be clear, there seems to be two separate schools of thought going on in this thread, one being an electrical issue and the other being a vacuum leak. I am 99.9% certain that my issue is vacuum related. The truck stumbles at startup, especially when cold (it acts just like it does when I pull the master cylinder hose off for seafoam treatments). This, combined with the rich fueling condition indicated by the CEL along with the traction control/stabilitrak issues, is a sure sign of a vacuum leak. I have not been able to source it yet...everything associated with the intake looks fine and is clamped down tight. I think that something else must have popped off when the tube came off of the throttle body, but I'm stumped as to what it could be. It's been frigid here the last few days, sub zero temps...not really conducive to garage work. It's supposed to warm up a bit this week, so once I get this ironed out I'll post back with my findings.
 

strokinpower

Full Access Member
Joined
Apr 23, 2013
Posts
195
Reaction score
1
You can still pull it apart if need be without a problem but when clamped it just adds and extra bit of grab if that makes sense.
 
OP
OP
TheFuzz

TheFuzz

Idiot Police
Joined
Apr 30, 2009
Posts
1,022
Reaction score
39
Location
Spurbury, VT
Pulled everything apart tonight and did a close inspection. All visible vacuum lines appeared to be properly installed and un-damaged. I did notice a couple of things about the intake though:

1. The Airaid rests right on the radiator hose, which gets hot enough to slightly deform the tube over time. Not by much, but it's noticeable. I doubt it does much of anything to impact the performance of the tube itself...but once your truck is up to operating temp, that heat is transferred directly to the tube. I know "heat soak" issues as it relates to intake tubes have been proven several times over to not actually be an "issue" since the air moves so fast through the tube, but I still wonder about it in the back of my mind.

2. Upon removing the rubber collar holding the tube to the throttle body and looking at it closely under a shop light, I saw a thin layer of dirt built up in the area where the tube sits in the collar. That has to be where the extra air is leaking in. The design of the collar sucks...it's essentially a hose coupler with a ridge in the middle to separate the aluminum throttle body from the plastic tube, but what it really needs is a recess molded into it right next to the ridge on the intake tube side that will allow the lip on the tube to fit into it more securely. I thoroughly cleaned all of the surfaces and gave them a liberal coating of hairspray as suggested by Strokinpower (my wife's Volumaxx to the rescue), disconnected the battery (yet again...sigh), cranked all of the worm clamps down as tight as I possibly could get them, and let the truck cool down for a few hours. The result? No stumbling upon startup a few minutes ago. Progress!! :cool:

I didn't drive it yet so the real test will come tomorrow. Also, it seems to stumble the worst during startup after it's been sitting all night and the block is stone cold. When I start it up tomorrow morning, that will be a big indicator as to whether or not this issue is solved, then the next few days will tell the tale. I have to wonder if replacing the POS rubber collar with a nice silicone coupler would solve this issue permanently...

Another update to follow in 48 hours or so.
 
Last edited:

Jtl09

TYF Newbie
Joined
Dec 9, 2013
Posts
1
Reaction score
0
Location
Western KY
Keep us updated! My problem started after a TB cleaning. I have a spectra cai, I thought I messed up the TB while cleaning so I replaced it. No change, idle was still messed up even after several idle relearns done and driving it over 100 miles. I had the codes read at auto parts store and they said I needed a new MAF. So I replaced it with no change to the weird idle. So I took it to the dealership, they said I needed to return everything to stock and put another TB. I told them it ran fine before the TB cleaning with the cai and that I had replaced the TB. They wouldn't do anything else to it until I did that.
I think it's a vacuum problem but I have used a can of starting fluid and several inspections of all the vacuum hoses I could find without success. Hopefully something can be figured out here!
I forgot to mention its a 09 suburban 5.3 flex 2wd.
 

zunman

TYF Newbie
Joined
Feb 2, 2013
Posts
8
Reaction score
0
So when my truck was at the dyno for tuning adjustments, the display came up about the stabilitrac etc. They pulled some codes which basically point towards body control module communication or failure. The codes were :c0561 u0140 u0122
 

Forum statistics

Threads
137,710
Posts
1,990,177
Members
102,701
Latest member
vsaravia
Back
Top