Yes, but from what I gather so far in my studies The downstream sensor 2 should look much flatter…small adjustments over time. According to my graphs Bank 2 appears worse than bank one with the misfire on#5
Would the post cat O2 sensor 2 waveform show a bad/clogged Cat? Just learning how to read the waveforms so I can take another test run. Last test after warming engine and viewing at idle the banks had completely different downstream sensor waveforms
Correct, problem was not a symptom of any change. All has been there for some time driving off and on, not my daily, waiting for time to work on it between other work. Always have something to work on here.
Noid light on injector 5 was flashing at steady pace without problem and when plugged back in the miss decreased again by half of what was evident when unplugged. Time to start shopping AFM delete kits with a tune I’m guessing
Thanks for breaking down your testing methods and recommendations as well as why compression test may give false hope.
I feel it’s definitely heading in the direction of bad lifter. My main concern with full AFM delete and cam swap would be knowing the remaining engine life warrants the cost...
I was able to find the crankcase relearn in the innova 5610 today completed and drive 20 minutes no change. Also, valves would open and close seen in borescope. Unfortunately it doesn’t turn enough for good view of their seated position
Could it be not enough intake valve opening due to cam lobe and pulling fuel? We may find out. I am waiting on a noid light and may be out of other options to check
All the injectors, plugs, and wires were replaced, gave a rundown of all the usual suspects have been swapped then replaced and am down to wiring other than what has been shot or internal failures
Ran a cheap poor resolution borescope down #5 and could see most piston head with seemingly little carbon build up and no visible damage. Ran crank over and both valves came out and reseated.
Definitely looking up CASE relearn and checking if I have capability. I have had battery removed for long periods of time between maintenance, even tried throttle body relearn by cycling key on off 3 minutes on/60 off 3 times then idle for 5 min and drive cycle?? Don’t know if correct but...
Will see about checking deeper into harness if I can find the schematic, shooting power and ground at injector harness and coil were solid? If I find connector and pins on ECM I could take off and shoot Ohm readings looking for jumping around when wiggling harness wear worn. Got noise light for...
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